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7/24/11

The front amp continues to not function. I did find, however, the elusive SpectraSonics amp setup, so I can send or give them to Greg at Monolithic. I will call him tomorrow and see what his schedules portends for a visit here. If he is another few weeks out, I will pull the dually front amp out and send it along with the SS stuff to him.

Randy feels I need another AC outlet in the truck, so I will reconnect the passenger side later this week.

 8/7/11

There are two leaks in the cooling system: 1-the oil cooler at the op, likely the gasket and 2-something at the lower left of the radiator core. This leak is not observable, as the fan and shroud shield it. So this whole assembly must come out for a look. Meanwhile, I carry a gallon jug of water with me at all times.

 8/8/11

Kelly and I pulled the radiator/intercooler out, and we see no obvious point of leakage. Sam from Allstate will come by in 30 minutes and pick it up, as I don’t want to grunge up the Tbird.

I am about to pressure wash the engine compartment, and look for the core support bolts which I believe to be loose. This may require sliding the condenser out.

 It did not, but I did have to do serious surgery to expose the driver’s side bolt. Kelly and I tried for HOURS to get it loose, even using a propane torch to melt the nylon in the nylock nut. No good. Kelly wanted to remove the bumper bracket (a killer thing in its own right), and I finally said no, went under and in 5 minutes cut the bolt out with the grinder and cutting wheel. I found a correct length 7/16/ x 14, put on some upper washers, and bingo! Done.

I will leave the opening I cut in the vertical member of the core support, as it now allows-AS IT SHOULD HAVE-for access to remove the bolt EASILY. I may expose the right side bolt as well at this point.
The radiator had 13 cuts in the left side from the fan shroud. So some serious thinking will be needed here to avoid a repeat and not only an $80 fix, but a new radiator for $250 plus labor.

Kelly and I were elated that we got the f---n bolt out. Perhaps this will cure much of the front end rattling.

I will take the truck to DPS for whatever is required to seal up the oil cooler gasket. I am DEFINITELY not going to attempt it again this time!

 Hey, the truck is a keepr, so I gotta make it work.

 8/23/11

I drove 50 miles one way this morning to Ventura to Coast Driveline, but Mark was intolerant of my 42 minutes late arrival due to traffic, so booked TWO other jobs in my place. Mighty fast work on his part! I drove home, and removed the driveshafts and took them to Cannon in North Hollywood. He is a strange guy. His office looks like someone backed a truck full of driveshafts up to the door and hit the dump button. He is a driveshaft hoarder. Perhaps I’ll take some pix tomorrow.

Anyway, he claims my front shaft is very heavy, and might be a balance culprit. He will let me know tomorrow. This half was made by Wenco 5 years ago, and appears to be quite overkilled, and not to much benefit.

This could end up being $400 if he replaces that tube. The rear U-joint was starting to wear.

Oh boy.

 8/30/11

The whole thing came to $240, and made no big difference. I will have the wheels all balanced individually, and see if that helps.

We put it up today on the rack (on its maiden voyage on the new casters), and used about 4 cans of degreaser, power washed the WHOLE underside and engine, and serviced the air cleaner.

 9/7/11

I had Flip’s check the wheels and tires, and they found nothing. Still some vibration.

Power Brake Bob came by yesterday to do the Impala brake line bleeding, found some adjustment issues, and got the Impala working great. He stayed last night and found two or three issues with the dually:

1-the right wheel bearing was WAY loose. He and Kelly got that wheel off, greased, and back on. Bob says the brake pads in front are charcoal, so we will be replacing those shortly.

He sees there are two proportioning valves on the brakes, and feels the rears are not properly powered.

On the way back from some errands, the truck started to heat quickly. We pulled into a Chevron, and after 5 minutes of frustrating dribbling of water into the radiator, I looked under and saw the lower hose was not on!!!

I bought 3 gallons of drinking water and 2 gallons of coolant, a total of $46, and with patience got 4.5 gallons of liquid back in, SO FAR SO GOOD.

Utterly amazing.

You gotta be alert to EVERYTHING.

 We got back here, bought some brake pads, and Bob found the right front rotor had spun the inner wheel bearing, and was still sloppy. Short story: NAPA for $157 for a new rotor plus bearings and seals, totaling $202. Otherwise, a 2-day wait for a $50 rotor from AutoZone.

Bob REALLY knows his stuff. And his innovative skills are not limited to brakes. He has some really good ideas on the KK.

 

The dually brakes are better: higher pedal, more pressure. However, the out-of-round rear drums are now showing themselves. So I need to have them turned, maybe tomorrow. The replacement of the wobbling rotor seems to have cured the freeway vibration. So I replaced tires and rebuilt the driveshafts, only to find it was the rotor.

 9/12/11

The entire front rotor assembly was replaced, as now are the rear drums, another $300. The pulsating stopping is worse than ever, the pedal is lower, and the truck hops around under hard braking at speed.

Bob will not return until at least Thursday. I need to get the right rear emergency brake cable replacement in hand before he comes. I will try Kay Distributors tomorrow for that.

We will probably replace the left front rotor, to make this an ALL new brake system.

 The 5 gallons of coolant disappeared without any sign, rendering the truck temp to a stunning 226 degrees. I refilled it again, have been driving literally watching the temp gauge, and monitoring the fluid EVERY time I get in the truck. It dropped about a half gallon, and now seems to be holding fine. I have not found any explanation for the vanishing 5 gallons, but AM carrying a fiver in the back just in case.

 9/17/11

Of course not a single rise in temp, using no water, but still carrying the fiver in case.

Bob Sweeting did work on the brakes, and they got worse. It turns out the new right rotor assembly is not true. We took off the rear drum assemblies today and had them turned. Still wobbly. Bob then pinched off the right front wheel caliper hose and we took a test drive. That showed the left side NOT wobbling.

We reversed it, and the right side showed as the culprit. Mind you, this is a NEW $200 rotor assembly. We will turn that one Monday morning at Brake Masters (they did a good job for $20 today), and hopefully that will end the matter. I got a brake pedal rubber cover, so that looks and feels nicer.

This brake thing is approaching $1200.

I still have three rotors to return Monday for about $400 cash.

 9/19/11

Drove over to Brake Masters, and they wanted $150 to pull off the wheels and turn both rotors. We took them off (well Bob did), and they turned them for $30 for the pair. Bob got it back together, and says the surfaces need to seat in, but otherwise all is good. I still have to locate a right rear e-brake cable, as the CarQuest repair cable was of now value.

Bob suggest going to the dealer, which I will do tomorrow on my return-the-rotors run.

 12/3/11

Still have not gotten Nick to do the fender work on the dually.

JJ and I went to the NHRA Museum today for a fascinating panel discussion on the last day of Lions Drag Strip.

On the way home we stopped in Hollywood at Musso and Franks for dinner. We parked around the corner on Las Palmas, and came out to find the truck TOWED.

We walked about a mile and a half to the tow yard, and for a mere $225.50 PLUS $68 for the parking ticket, I got the truck back.

RIDICULOUS!

The sign is not well posted, and it turns out we got there JUST before 6 PM.

 2/25/12

I have blown off the lower radiator hose three times in the last few months. I had Kelly double clamp it a week ago, and it popped off two days later in the driveway. Either there is great air in the system, or a head gasket is pushing pressure in the system.

I will contact DPS on Monday for an opinion.

The radio/CD is HORRIBLE in its loose-ground symptom, and of course the non-working front amp. There is AWFUL alternator whine in the system. So sad that Rob Anderson no longer will pay attention to the car projects. This and the condor are in big need of hifi help.

 2/28/12

I left a message for John at DPS.

The puke tank was empty this morning, needing about a gallon.

Strange.

 3/17/12

John took it for two days, and all he did was drive it about 5 times around the block to purge the air in the system. He claims no other issues exist. I brought it back here, and a week later it has not overheated, but has a drip under the oil cooler. I’ll top the puke tank off and keep watching.

 3/21/12

So today it blew the hose off again. We had water on board, and got it back on in short order. John now asserts that his previous two possible causes are NOT the problem, and that the inverted radiator and the low puke tank are to blame. How did this thing work for 6 years then? He asserts that it must be making steam.

I have mocked up another puke tank to go further back and higher, and I will go there tomorrow to show him and get his thoughts.

I predict that I will make this thing, and it will not solve the problem.

 4/9/12

I have not made the elevated tank. I may just put a gallon bottle on the hood temporarily.

I am losing nearly a gallon a day.

 4/16/12

I think I will in fact do the elevated take-off-the-hood reservoir thing. This will at least end all conjecture about the low reservoir being the issue.

I’d love it to be the cure.

 But I really think something else is awry.

 I corrected the utility plug today by removing the ashtray system, tightening up the plug barrel, and checking a few other wires in the area. The gas gauge doesn’t work, and I have no idea how to connect it other than how it is right now. So I removed it, and am using the space the store my I-phone while charging it.

The driver’s door strap pulled through, so another must be found or made.

 4/19/12

I went by DPS and talked with John Hamlin further on the cooling issue. I ran by him my idea of another upper tank, and he thought it was good.

So today JJ and Kelly and I hooked up a tank in the center at the firewall, over the turbocharger, and teed into the smaller of the two lines from the puke tank. We removed the hood for the exercise and to allow the tank to sit freely.

The truck appears to have lost no water on its drive today. We’ll see tomorrow.

 I intend to run it for several days, and see if it maintains its coolant level. If not, then we need to look elsewhere.

 Nick says he wants the truck this weekend to do the bodywork. I have the missing lower piece of one fender for him.

The hifi front amp has come on a couple of days in a row at startup, then quits. The right side battery positive terminal was a little loose, and I put a different bolt and some washers on that connection.

I checked the oil and no sign of water in the crankcase.

 5/7/12

Nick promises he will take the truck on Wednesday 5/9/12.

Sure.

I towed the KK to Gardena, and the darn thing overheated coming over the pass. I made it home, peaking about 221 briefly, and spending some time around 22-217.

It took almost 4 gallons of water. The capacity is around 5 gallons.

Not good.

So while the higher puke tank is doing SOME good, there is clearly a more fundamental issue.

I’ll report this to John Hamlin at DPS tomorrow and get another look at it schedule for soon.

 5/9/12

John reached his race expert guy, named Guy, and this fellow said something is broken somewhere in the motor, and the engine must come out. This could be a cracked block, bad heads again, whatever.

This is expensive news, though not unexpected given all of the previous stuff mentioned above.

So next week it gets the big deal over at DPS.

 Nick has not taken the truck yet. But who knows, he might get it all done before I get it over to DPS.

 5/26/12

I replaced the crushed muffler from the rack accident months ago, for $170, and unfortunately this did NOT cure the heating. I then drove to Allstate Radiator and Sam said the radiator was certainly not clogged, so that takes that out of the picture, too. I did a test up Woodley hill, going full throttle for about 6 seconds, and the temp jumped 12 degrees within 15 seconds.

So it is almost certainly a cracked head again, a $4000 affair.

This will tap me out on all fronts.

I bought a little beater truck to trade away for some landscape work here, and am thinking maybe I should keep it for myself.

 6/20/12

The beater is gone on the landscape trade, and driving the dually works if I never exceed 900 degrees EGT. This is TOUGH to do. But doing that allows me to let it idle indefinitely with the AC on (but the AC will freeze up eventually), and drive VERY tamely on mostly flat ground. No hills of any consequence, except at low speed, including never-before thought-about little hills on the freeway, etc. Sepulveda Pass is daunting and challenging, and SLOW.

I went out this afternoon to attempt to correct the front amp not turning on, using the zener diodes supplied by Greg Schuk of Monolithic Sound.

NO GO.

I also found the subwoofer amp nearly flaming at 201 degrees of heat sink temp!

Holy crap!

So that is coming out and being shipped tomorrow to Greg, along with the front amp, and two other amps I have here.

The truck also has an odd vibration (we’ve talked about this before) between 60 and 70. It is not always happening, sometimes not when first starting out on a cold motor.

I have replaced the driveshaft, changed tires, replaced the right front wheel bearings, had it aligned and balanced, and this is still happening.

Obviously I have not found out what it is as yet.

I got a compliment today at lunch from someone who had not seen the truck, asking if it was a new truck.

This has been said many times before.

Not quite, but thanks.

Nick is going to need at least a week to repair the fenders, once he gets to it. I need the Bird running for that.

AND, the engine repair will likely be a two-week deal as well.

I found two labeled wires/fuses hanging down near the fuse box, one for instrument lights, the other for the fuel gauge. I will plug them in later and see what gives there.

 6/28/12

So far plugging both wires in results in no change. So there must be a fuse in line to the radio.

DPS is pretty much moved now, and tomorrow I am hoping John can take the truck in and start on it. I got the Bird back today in drivable condition, but not completely repaired, and that will work fine for now.

 6/30/12

I tapped into the white fuse panel, the one with all pins and no fuses, and found some hot pins. I put push-ons on three wires, and had power to the radio and charger plug. But now the radio does not come on.

More checking to be done.

DPS is supposed to be taking the truck Tuesday 7/2/12 to correct the cracked head/overheating issue.

The front and woofer amps are out and in a box, ready for shipment to Monolithic.

 The puke tank mounting broke on the right fender well, so a little touch of welding will be needed there.

 7/7/12

The truck is at DPS since Thursday 7/5/12. John says it will take a week.

 7-10-12

I saw it yesterday afternoon with Jerry. John was not there.

The cylinders have heat marks at the top where the rings are at TDC, and some striping about 3/4” wide down the four right sleeves at the same place in each of the back three cylinders on the right bank. Hamlin feels THESE are the terminal damage indicators, and says the marks at the top of all the cylinders are machining marks. But NONE of that striping is on the left bank.

I am scared I need a whole new motor.

 7-13-12

I have ordered an 80K mile used motor from Florida for $5650. It will run over a thousand to install it plus some parts. So this whole thing is looking right around $7000. This will virtually clean out my bank account.

Time for some paying work.

 7-18-12

The engine arrived today and I JUST scraped together the $4K for the motor in cash. PBB required a little prodding to get his $1600 in on time. I purchased a used motor from Florida, then canceled it. They have not refunded the $5650. So I was down to very little in my account, hence the critical nature of PBB’s funds being in on time.

This place offered an option of no core for no warranty. I might just consider that.

 7-21-12

In apparently typical fashion, the used engine has a defect. It appears to have been hit in the pan rail area. Repair to this area would run about $3K. The seller asserts there was no damage, but I put him directly to Hamlin to explain the nature of the problem. My expectation is that I’ll see another motor here come Monday or Tuesday. This puts completion of the dually out at least 10 days from now.

Additionally, the original $5650 done by VISA for the first motor from Florida has still not been credited, so my bank account is at a few hundred dollars.

 7-28-12

The repaired used motor got returned to DPS yesterday (Friday), and John says look for around Tuesday. I’ll presume Wednesday at the earliest. I am getting a new water pump.

As of this writing STILL no refund from Florida.

I may call the attorney general there on Monday if this credit is not completed by noon on Monday.

 7-31-12

Today is Tuesday and John has not started on it yet, having to pay attention to another larger job first. He will start on it tomorrow, and now predicts Friday for completion.

The Wells Fargo credit has not happened, and WF has called me today to say they left a message for Brigman. If not answer and confirmation that Brigman will issue and immediate credit, they will file the complaint, refund my money, and hope that the complaint stands. WF gets only one change to move on a complaint, so they want to be sure they are good on it.

 

 

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