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10/6/08
On July 4th, 2008, I blew the left front tire, despite the fact that the car had been pulling harder and harder RIGHT for almost a week. I replaced that tire with a matching tire on that date.
For the last week, the truck has been pulling right again, and has had a serious shake when I first start out, smoothing out as I reach freeway speeds.
But it was freaking me out, and I held to the right lane for the last few days.
I was on my way over to Mike’s Frame today to get it checked out, and called him on the way. I suggested perhaps I should go to Tires Buy Mark (yes, correct spelling), and he agreed, warning me they would undoubtedly tell me they could not match the tires and would try to sell me two new fronts.
I then recalled I thought I had bought tires from Flip’s. I went there, and Tim corrected me noting that my fronts were NOT Hankooks, but Laredos. The rears are Hankooks, all 4 of them.
I asked if he had Hankooks, and he said yes and could have a pair on in an hour.
I used the new Laredo left front for a spare, although at this time I have NO rim or hanging hardware. So for $270 out the door, I have now ALL matching Hankooks, all in good condition. Perhaps I got the Laredos at Guadalupe Tire or Jalisco Tire down the street. They were probably WAY old tires, as they both took a crap close to the same mileage.
The truck feels WAY better. Now to cure the front end clunking noise. I am supposed to go to Tyreman’s tomorrow for that $500 repair to the A-arms. I’ll call Joel and ask a few questions first. I’m not sure I can do that right now.
The dually runs great, hauls with the Edge hooked back up, although I am not crazy about the lesser low end performance. John talked me through programming it for low end performance, but it does not seem to be doing what I asked.
I’ll stop by DPS and see if they can straighten it out and turn off the 71 MPH speed alert.
Mike, from Bob’s Big Boy, has still not stepped up notwithstanding dropping the price to $17,500 last weekend while I met him there.

10/11/08
Mike is not ready to buy the dually, despite all the talk.
I took the truck to Flip’s and they can find NOTHING wrong in the front. Time says it looks all new.
I attempted to go to Bakersfield today for the races, and the truck started smoking just as I got to Roxford. I checked the Edge, cut it back to ZERO setting thinking MAYBE it had gone into a too rich fuel setting, but still saw some smoke.
I pulled off the 5 onto the 210 and immediately exited at Yarnell, and as I pulled to a stop the trans downshifted with a clunk. I KNEW immediately what had happened: the crappy little spring clips that GM uses to hold the lines in place on the radiator let go. This is the third or fourth time on two trucks this has happened. It was for this very reason I spent a LOT of time and money having Brett put a sensor in the line, which turned out to be useless, as the pressure at idle drops to near zero, and at peak is about 35 PSI. Sure enough, trans fluid is EVERYWHERE, including the rear of the truck. I had it towed home, bought two cases of BrakeKleen, used three cans to wash it down, and now I’m going to go out and start snooping.
12/29/08
Had an odd thing happen today, and not cheap. The dually has two tanks, connected by a common tube. There should be NO air pockets, given the size of the crossover. But, the lat two times I filled it, I could only access the right tank, as I did not have my gas cap key We’re gonna get rid of that locking cap tomorrow, as previously promised.
Anyway, the fuel gauge showed near empty a few days ago, and I refilled, only to find I could put no more than 18 gallons in it.
It showed empty again this tie, with about 300 miles (the same), so I said no stop. MISTAKE!
It ran out on the freeway, and I coasted down the Desoto (east) off ramp and made the corner, pulling right up behind a CHP, who was writing someone a ticket. The short story is the CHP pushed me (with his car) into the Shell at the corner.
I filled it, again only getting 19.6 gallons, essentially EMPTY on the right tank. But why is it not filling the left?
It then would not prime, and would not start. I got a ride home, a ride back, opened the left side tank locked cap, but no massive escape of air, and the gauge did go down to a little over a half tank. HOWEVER, the fuel level remained at the top in the right tank!
I had to get it towed, and AAA refused to tow it. Mind you, they’ve towed this vehicle perhaps a half dozen times in the past few years. No, no, not this time. So I will be gong to AAA to add RV coverage. Utter bullshit, plain and simple.
I tried to get Harry, but he was booked for the day (about $45).
I then called Frankie at Creative, who had me call Jose. Jose towed it, and then tried to hit me up for $100!!!
I had Frankie call him, saving me an entire $20. I will NOT be using Jose again.
John and Jerry at DPS took the primer apart and after about an hour go tit primed and running. VERY odd. Naturally, I will NOT do that again.

7/24/09
The front end has not been cured, notwithstanding I have been back to Mike’s a couple of times for realignment. We did more relieving of the center link, and sadly it managed to get out of alignment scrubbing about half the life off a brand new set of Hankooks in front. The clunking continues, but otherwise it seems to be holding the alignment for now. The truck runs great.
I got the hifi FINALLY fixed and had the subwoofer amp rebuilt at Monolithic, and the front speaker 4-channel amp checked for a couple of months at Monolithic with no apparent problem. I had Greg build me a high pass filter for the rear door speakers, as they share the EQ‘d bass signal to the subs. I installed this filter ahead of the electronic crossover to the rear doors, but Greg says it won’t work that way. So I will re-wire the in and out AFTER the xover and put it only in the low pass circuit to the mid-bass speakers.
All said, it is nice to have a substantial sound back in the truck.
Every time I go to Bob’s, Mike inquires about the truck, but obviously has no interest in it. And, I have3 dropped the price from $22K down to $13,900. I just have no idea what his supposed interest was all about. I mean, I took him and his friends for rides in the truck, and he asked week after week about it, came out and saw it and the other cars here, etc.
Whatever.
It is clear that NOTHING is selling for what I am asking. I have dropped the price drastically on several cars with no sales. I will just have to ride out this economic crisis somehow without selling 5 cars.

8/12/09
I have not altered the rear door xover yet. I had FOUR things go bad AT ONCE:
1-the radiator leaked, so I replaced it
2-The oil cooler, integral to the oil filter, leaked and John at DPS kindly gave me a new unit FOR FREE. It has a TINY drip now (water). I had noticed sludge in the puke tank.
3-The truck would not run (it did for ten seconds then shut off) after we did the above work, due to the bunged-up oil pressure sensor pins and plug. I hard-wired it and FINALLY got the truck to start by priming the hell out of it.
4-The fuel system was not holding a prime. There was a pinhole leak in the hard line just under the driver area. I replaced those lines with blue line to the motor.
It now works.
WHEW!

A fellow in Arizona expressed strong interest in the truck, citing he would call in a month after his crop-dusting season ended, and would fly into Van Nuys to see the truck.

Jay has yet to correct his dash work.
I found a loose core support bolt, and tried some shim work while we had the radiator and intercooler out. We shall see.

9/6/09
It took Jay 10 days to do the dash. He took my advice and removed his second bondo attempt and fiberglassed the panel, then painted it. Once back, the radio was not installed, and the AC quit a day later. It turns out the AC blower motor died (and had been expiring for quite a while). This was BRAND new three years ago. I got a new one for FREE at AutoZone on its lifetime warranty. My engineering on removable wheel well access panels proved critical. Of course I could not find the ONLY size socket/wrench that would work on the screw a 9/32 or 7 mm. I bought a 7 mm ¼” drive socket. Bingo, we have air. The stereo works, but NOT the front amp. It’s too friggin’ hot to sit in the truck testing for now. The subs and rear door speakers work, so at least I have sound. All items are fixed, and I have just not pushed the hifi into the sleeve locks as yet. The truck is apparently now no longer leaking in the area of the oil cooler. It still is purging some oil out of the tank, though. Not puking, just bringing residual (I sure hope) oil to the top.
I also found a couple of spare horns, and mounted those in the right fender area. I just have to find the horn wire to get them all working.
I cleaned up the interior, REALLY cleaning the dog hair and dust from the seats. So no rides for the doggies for a while.
No word yet from the Cropduster.



9/7/09
I broke down and took the dogs for a ride today. So I will have some vacuuming to do. Gotta have fun, you know?
I need to get on the front amp thing early in the morning when it’s cool.
I talked with Rob Anderson regarding trying to purge the remaining oil sludge out of the cooling system. He said not to worry about it, as it will naturally just rise to the top. I found some in the bends of the hoses when we changed the radiator, so I’m figuring I might be losing a little flow in the evaporator or in some of the lines. The dash temp gauge does not read the same as the computer readout on the Edge at all times, and that makes me a little suspicious that the sensor is greased up. I may try some surfactants to solubize the oil and then drain the whole thing and flush it. I’m really running around taking off any hoses again to inspect. I will just have to go that route I guess.

3/3/10
I did not solubize. The truck seems to be running quite cool now, and an oil leak at the trans cooler (just an O-ring) has been solved at DPS. The EDGE computer crapped out once again, and for $100 I got it replaced. Runs great again.
The amp thing turns out to be something I deduced: the turn on sensor does NOT like anything over 12 volts. So on charging, it shuts off. Greg at Monolithic sent me some zener diodes, and I will install them soon. I will also relocate the rear door speaker sub filter as directed.
No word from the crop duster. I advertised for a few times in Craig’s List then stopped.
I am taking the truck to Creative for some minor paint touch up, and just putting no expectation in selling ANYTHING right now.
I continue to take the dogs around, and vacuum the truck out every couple of weeks.
I have not seen Mike at Bob’s (who over a year ago was so hot to trot on the truck). I am looking to get a heat pump AC unit for the house from him.

The steering continues to go off, and I replaced the front tires. I called Tommy Lee, and am due to call him again to look it over. The wheel appears to have gone out of adjustment after about a month. I must get to him soon, before I scrub these tire off, too.

4/6/10
The steering is off, but now it is in the steering column. It appears the knuckle joint on the tilt wheel has gone WAY loose. Roy is returning tomorrow to finish opening the column (he needed something to access the snap ring holding it all down), and I hope we find nothing broken, just loose.
The hifi is now working on front speakers, and I have not installed the Zener diodes, nor relocated the low filter in the system to the rear doors. But, soon.

4/7/10
Roy came today and it took him 6 hours to repair the column. Turns out a snap ring had popped off the u-joint in the tilt mechanism, and could have resulted in NO steering. Whew!
Roy will return tomorrow (his regular day) to put two final boot pieces on the column and address other matters on the 92 Tbird.
 

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