Diary
Page 21 - 7/26/11 to 4/16/12
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The right side, more
finished, took a lot more work, and LOTS more cutting and grinding and
drilling to get apart. We’ve basically established the proper height for
the right side now, and JJ will return in the morning with some 12 mm x
1/.75 bolts, which will have their heads cut off, and the shanks welded
to the frame to receive the running board brackets. This will open the
rear fenders to some modification, the running boards themselves to
further refinement, and give me a stopping place for the front clip to
rest.
7/27/11 JJ got 7/16 x 14
bolts instead, just fine. We welded the studs in place, and after
several on and off the truck fittings, got the right side looking good,
bolted in place, and with some backing welded in for one of the front
area bolts.
The left side needs
the brackets drilled and four studs welded in the same fashion. The left
side panel was reset for appearance and as a template, and today JJ and
I got a 4 x 8 x 3/16” foam board to make templates. We made both side
panel templates, set them in place, and did some fiddling with the rear
fender interface to the running board surface.
The right side front
clip interface is already in front of the running board. The left was on
top, and we have slid the surface metal back to allow it to allow drop
down to the running board bracket as a stop. The front clip has “darts”
welded in to continue the body sculpted lines onto the hood area. As
received from Joe, the left side has markings and an arrow indicating it
must go UP, the right side markings showing DOWN. We will cut the right
side with a grinder, and the left side can be built up with weld or
bondo at the appropriate time. The truck looks MUCH better with the
correctly aligned running board lines.
8/2/11
So those are the
rear braces, and the mocked up assembly is shown above. We now have made
the front half supports, which are more complex. We created a ¼ x 2”
band of steel along the cab bottom on the left, and connected the
existing brackets in the same way on the right.
We welded studs to
them, drilled the body in 5 places each side, and bolted the ledger to
the cab. We have the outside rail in place, and are now making the 10
brackets to hold up the outer rail, welding 1-1/2 x 12” and shorter
pieces, 5 per side, from the ledger to the rail to hold the down force
on the whole assembly, Looks to be very strong. We were quoted $185 and
THREE weeks to have 10 pieces cut at Industrial Metals. We will flame
cut them tomorrow from our stock, and finish them with a Dumor grinder.
8/4/11
The torch made for
rough cuts and lots of slag, so we ended up using a die grinder (cutoff
wheel) and a Dumor to do the running board braces. We spent yesterday
and today fudging the whole left side system around for level (in to
out), and alignment to the bed (front to back height). We cut apart the
fro nt bracket on the rear half of the board, as Joe had made it going
UPHILL (not square). So we have done MUCH cutting apart, remaking,
rewelding, etc. The pix below show the left side running board structure
as it is now. We are garage builders, not a CNC million-dollar facility.
I will have to live with my own limitations in technology and craft. But
I gotta say, what we’re doing looks pretty good to me.
It is within 1/8”
all the way, the lower panel below the bed is PERFECT now, and now we
can address adding some serious stiffening at the front corner by the
cab. I will likely add some metal behind the cab sheet metal, and add a
¼” steel tab to extend the front corner to receive an additional brace
there. This may also act as a stop for the front clip when it closes.
The left side looks wonderful now being straight and plumb.
We have dressed the
welds, and I intend to do some priming of the raw metal, perhaps even
tomorrow, to retard rusting and the eventual further grinding, etc.
I felt very good
about the three of us pounding, cutting, grinding, and fabricating over
the last week. Jerkoff Joe could have done this SO easily. But NO, just
deception and idiocy were the order of the half decade with him. I will
put a call into Tammy Allen’s attorney either tomorrow or Monday, and
see what they are doing (or not) with their own Joe’s woes.
We added ¼” bracing
to connect the separate bolted brackets on the right side, so have a
continuous ledger on that side as well.
I think I will cover
the running boards with a rubber mat, custom cut (CNC process), with the
KiloKub logo in red against the black rubber background.
8/7/11
I spent a few hours
today, Sunday, mocking up the exhaust and front radiator group. The
exhaust will cross under the frame rails directly behind the cab in a
box-affair about 5” deep so as not to be below any other hardware, about
12” long to get it from about 5” inside the frame rails to 6” outside
the frame, with another box atop the outer portion another 5 x 4 or so.
This upper box will receive one end of the Aero turbine shorty
straight-through 4” in and out muffler. Aft of the muffler will be
another box, about 6 x 6 x 24 to carry the exhaust either out the side
of the panel above the running board, or a down outlet and just a
non-operational 12-outlet escutcheon on the lower panel.
The radiator pack
fits nicely under the hood at 13” high, 34” wide and about 13” deep. As
noted previously, some sheet metal work on the underside of the
hood/front clip will extend down to seal off these radiators. This will
be a 4-unit affair, with fans either mounted on the insides of the pack
with shrouds, or fan above or below to pull air through the assembly.
Kelly and I looked
at the running board stiffening plans, and adding an inner backing plate
of ¼” steel will help, but we need bracing to further stiffen the
assembly so the bolts and plates don’t just soda-can the rocker metal.
At the rear of the
running boards, the refined brackets are still flexing. I will add lower
back-braces (facing the center of the truck) to these brackets with
bolting up into the bottom of the frame rail. This should take care of
the flexing. If not, I will lengthen the gussets.
The left front of
the running board needs a second brace closer to the front fender, with
another bolt through the very front portion of the side of the cab
rocker panel.
I am close to trying
an Electric Life crew jack pair on the front for opening and closing the
clip. I would imagine some air struts would assist in all this. I need
to come up with some alignment and receiving stand on the cowl/firewall
with matching pad on the fender/clip. Many tilt hoods have a backward
sliding latching mechanism. This does not appear to be necessary here.
But some sort of alignment and down lock will be required. It could be
as complicated as a micro-switch and another set of EL jacks to pull it
down, or a latch system powered by the shorter jacks.
Tomorrow will see
some temporary braces to hold the muffler and mockup boxes in place, and
some research on shorty headers.
8/15/11
We did some serious
work on Friday, and all day today as well. We pulled the running boards
off, added the “joists” from the ledger to the outer tube/rail on the
right side, added a second piece of 3/8” x 1-1/2” to the bottom of the 4
rear angle braces (much stiffer). Straightened out the right side sag in
the middle and then spent the remainder of the day finish welding every
joint full-length, and grinding all of this down flush. These pieces are
starting to look real good. The back braces work GREAT, and we did
lengthen the gussets as well. So we have done three stiffening actions,
and all have paid off nicely.
Tomorrow we’ll
attack it for perhaps an hour, then I have to go to a bid in downtown
LA, while JJ and Kelly run to the Rodriques job.
We’re getting better
at this, and making progress. This is way more than could ever be said
for Joe. I have not yet called Allen, but will do so tomorrow or
Wednesday if I can remember early enough in the day. I’ll take some pix
of the full running board assemblies off the truck after we finish
grinding the welds tomorrow. I intend to primer them.
8/18/11
Another day has
slipped by without calling Tammy Allen. Perhaps tomorrow.
We worked EARLY at
Rodriques, shoveling dirt and carrying HUGE lumber, and got back and
started on the KK at 12:30 PM. The running boards remain bolted in
place, and are strong as stone, and we were working until after 5 PM. We
worked on the lift system, snapped a few nuts and bolts off in the
process, and came up with a 3” circular tube mounting for the top
(thanks to a suggestion from Kelly), and JJ has fabricated two of those
tubes. We tested one, and it is correct. We are modifying it to be a
little less tall than its current approximately 2-3/4” by about ¼”, and
we’ll be cutting a ¼” thick cap to go on it, through which a ½”
shouldered bolt will reach a nut welded to the inside of the new fender
well ¼” steel plate. We snapped this welded nut off today doing a test.
It will work fine when re-welded (properly), and when be used as a
receiver for the “axle” bolt, and not tweaked sideways under 300#
pressure.
I’ll shoot some pix
tomorrow. We have to make a similar “can” for the bottom mounts, and
then we should be good to use the air rams. I will ultimately have to
hook up the control panel I made. But for now we could just give them a
squirt from the air compressor to function.
8/20/11
We made the lower
can, and I have it temped in place. There is still a little trimming to
do to clear the air valve on the ram. I will need to go to Numatic
Engineering (I hope they are still in Glendale) for a compatible ¼” pipe
fitting street “L” to turn the fittings parallel to the ram. There is
another “air actuator” shop at Victory and Burbank in Glendale as well.
The design looks
cool to me with the round “cans”.
8/23/11
JJ and I went to
Numatic in Sun Valley, then right down the street to Industrial Metals
and got a 3’ length of ¼” wall 3” diameter tubing. We started with
cardboard tubing, graduated to muffler tubing, and now our REAL DEAL
stuff is mondo-thick ¼” wall.
We have had to
relocate the mounting nuts a few times, as we discovered this morning
that relocating the lower nut upward put us back in interference with
the water pump outlets, notwithstanding our low-profile cool Numatic
“L’s”.
JJ and Kelly are
grinding on the lower cans right now, as I have just welded the lids on.
We need one more
mounting nut for the passenger side, which we’ll get in the morning.
As soon as Kelly is
done dressing the longer lower cans, I’ll weld in the driver’s side. I
did some touch-up welding and dressing, and welded the can in (the upper
part for now as the lower part requires lifting the truck up. I cannot
push it back onto the lift without Kelly or JJ, and now the lower part
of the ram housing is hitting the lower cutout lip of the can. I need
now to relieve about a half inch of that lower opening to allow the bolt
to find the nut easily (which it does without the ram in place), and
will do so in the morning. We have PLENTY of lift height from the rams
as set now. They will actually lift the bed about 7” higher than the
picture below.
I saw some cool
control modules at Numatic, but what I have should do just fine. I MIGHT
need a couple of control valves for the front system, as it appears I’ll
be using air up there after all. My former Funnycar control board has a
switch for the front actuation, but it was only single action, and I
need push and pull, and the associated valves.
It is exciting to be back in the creative and progressive mode
after a half decade of screwing by Joe.
8/24/11
I spent a LOT of
time welding today. VERY hot. SO much so that I was literally looking
out from under water, as my glasses started to fill up! I welded both
the top curves of the wheel well tub plates (1/4” thick plate), about 3’
on both sides, the bottom junction to the bed, another 5’ or so, and the
lower lift “cans”, another foot or so of weld bead. This is hot,
tedious, exacting work. My welding is improving, though I seem to have
contamination issues, as my welds look like lava volcanoes from time to
time.
By and large, I’m
laying down MIG welds that look like decent TIG “rolls of nickels”.
The three of us
worked on the lift system, made spacers, shortened bolts, relieved the
perimeter of the heim joints, trimmed two cans for clearance, and pretty
much got the system ready to receive some air and test it. I believe I
have enough fittings and some tubing to test it out. Tomorrow should be
exciting.
I asked JJ if he was
enjoying the fabrication. “No” was his answer. “But I’ll like it when I
see it work”. I relish ALL the work, and like him, am anxious to see the
performance. What we’re doing looks pretty good, shows thoughtful
workmanship and engineering, and I hope it shows well once done.
My other cars have
seemed to inspire the viewers, so that is comforting and reassuring.
8/26/11
Today JJ liked it. I
modified the old control panel from the Funnycar, plugged up some
orifices, went to Numatic for some additional fittings, and basically
hooked up the lift system as in days of old.
Worked perfectly!
Kelly was shocked
and amazed. JJ was not having fun, but was pleased. I did some long
thinking last night both going to sleep, and waking up. I came up with
two systems for the front. JJ and I tried the knee-action version, and
then I thought of a third way, while standing at Numatic. Then we came
home, and a fourth option presented itself, and that is how we’ll go:
18” stroke rams with about 120# of lifting power each at 100 PSI. We’ll
have about 125 PSI with the power brake pump. We’ve done some measuring,
and it looks good. We’ll go from the bottom of the frame rails just
ahead of the A-arms, straight up into the bottom of the hood and fender
junction. I ordered them today from Numatic for around $200 for the pair
(special order from Bimba), available in about a week.
JJ is cutting some
bracket material right now to allow me to pin up the mock-up foam tanks.
I’ll work on the
cold and hot water mock up tanks shortly.
A fairly immediate
concern is how to stiffen the front clip. The fenders flop like elephant
ears. The main point of flex is the junction of the fenders to the hood,
particularly at the rearmost portion of that interface. Randy suggested
fiberglassing the underside of the whole clip. This seems like a good
idea. He also thought some stiffening ribbing would be appropriate. I
agree. I will endeavor to design some ¼” by 1” backbones for that hood
to fender junction, and carry that around to the trailing edges of the
fenders as possible. There is, of course, tire clearance to consider
here. I’ll have to install some temporary struts across some points with
the clip DOWN, in order to insure it fits. There is also the tricky
interface between the rear of the hood and the cowl, an area not
addressed by Joe in his half decade of lassitude. While I would prefer
Nick to do this, I cannot wait for such largesse on his part. I’ll do my
stone age creativity as possible on this and get on with it.
8/29/11
I confirmed some
specs with Numatic today, and the rams are on for later in the week. We
removed the mock-up of the other proposed lift arrangement, cut off the
temp tabs, and launched into some stiffening of the front sheet metal.
I connected the inner grille framework support to the front sheet
metal along the sides, with only a small improvement in stiffness. We
are going to add ¼ x 1-1/2 strapping above the grille frame and attach
that assembly along the whole top rail, about 5 LF or so. This should
add some more stiffness. However, the fenders from the junction of the
hood back are floppy, so some ribbing coming from the nose area of the
hood and extending along the hood line under the fender junctions may
help.
AND, we have to get
the left front fender to tuck in at the rear and move tighter against
the cowl/body. There also remains a complete refitting of the hood to
the cowl, and there are several thoughts on how to accomplish this. One
is to extend the cowl edge and not mess with the hood (floppy) metal.
Another would be to add a ½” rod perimeter to the hood, and patch in
sheet metal (about 18-gauge). Nick has noted previously he is not in
favor of the extend-the-cowl approach.
I can accomplish
proper alignment by pushing on the fender, but clearly some structurally
correct alignment must be done. Whether this mean cutting and re-shaping
the fender or what is unknown. I SHOULD have Nick come over. He is
swamped, and not amenable at this time to such philanthropy.
9/1/11
Nick came by last
night, and we discussed at length his emotions about the project, and
his technical approaches to the hood, etc.
He suggest building
a “birdcage” to define the properly-gapped dimensions of the hood and
fender openings using 5/8” square tubing or round rod, then filling back
to the existing hood and fender sheet metal from the perfect perimeters.
I understand this
approach, and if Nick cannot bring himself to work on the truck, I will
do my best using that (pun intended) framework.
The KK is trapped up
on the rack right now as I am having the cylinder rebuilt which powers
the lift. It has lost a seal, and for $350 it is out, being repaired,
and will be back in tomorrow, ending the dripping onto whatever car is
parked below.
This is a MONSTER
cylinder, extremely heavy, and requiring very specific parts.
9/3/11
Jaime returned
yesterday and put in the ram.
All good.
JJ and I are moving
toward starting the “cage”. We cannot use 5/8” square tube, as it is too
high for the cowl interface. We’ll probably end up with ¼” flat bar
about 1” wide. I hope we can buy some, otherwise we’ll be cutting my
stock down, an arduous task.
I got the Numatic
rams, and they are about 6” too long. I have relocated the lower pivot
point back to my original rearward place, and it appears the opening
will be just right. I have to make a hood plate and eyelet to receive
the clevis on the rams, and once in place I will find out immediately if
the system cycles properly. I was grinding a tab down this afternoon
before I had to leave for tennis. I’ll resume on this in the morning.
9/4/11
I relocated the
pivot points back to the more front place, about 6” back of the very
front of the frame rails. These work for length. However, three problems
have arisen:
1-I dented one of
the rams when I closed the clip last night. It is a very minute
indentation, but enough to freeze the piston inside, so there went $100.
And since tomorrow is Labor Day, no one is open until Tuesday. This
looks like a Friday replacement at best.
2-The valving does
not seem correct, as the ram does not respond to the switching. I ran it
direct off the compressor, and the up function works. The down is hard
to assess, but probably works on the direct hookup as well.
3-One ram is not
enough to lift the front clip.
9/7/11
The valve was OK, I
had it plumbed incorrectly.
Bob Sweeting was
here and managed to get the dented ram functional. But still not enough
poop, even with both rams working.
I then worked out
the geometry with the longest electric rams I had bought for this very
purpose, and modified them with slightly larger holes, and mounted the
left side with the same heavy-duty “can” affair as the rears. Tomorrow
JJ will make the right side, I’ll weld the chassis nut in place, weld
the can in, and we’ll see how these work. Hopefully well.
9/10/11
JJ did make the
right side, and I mounted it intentionally higher up the frame rail, as
the measurement from the hood to the mounting point demanded it. I did
NOT account for the twist in the hood, which was being held by the left
side only. I had to then cut it all off, redo it, and remount it.
Works just fine.
Bob had noted we
should create a sliding pivot adjustment to get the hood assembly closer
to the cowl, which at present is about 1” away.
We took a more
direct approach and redrilled the pivot tabs an inch closer. The fit is
better, and will now require:
1-rewelding the
faulty nut Joe had put in the pivot arm
2-trimming hood
metal near the cowl.
But hey. Getting it
closer.
We may still end up
with Nick’s “cage” approach, but at least the front clip is closer than
before.
I had an unexpected
conversation at Bob’s tonight with Rich Almack, a former stereo
installer and car builder who noted Joe had screwed him on a trunk lid
repair. Basically the same crap as me, just smaller and quicker.
9/12/11
Kelly spent the day
grinding on the underside of the front clip. We, in fact, turned it over
on the ground so he was actually sitting IN it. He made a mountain of
grinding debris, and dramatically cleaned up the underside of the clip.
I did a little
dressing on the welds around the front “cups”, and they now look nice as
well.
When all this stuff
is bondoed and painted it should present quite nicely. The “cups” are
quite intriguing.
JJ and I took a trip
to Industrial Metals and got 20 LF of ¼” x 1” flat bar to make the cage
and the interior stiffeners for the front clip.
Here we go.
>
BRILLIANT!
Nick failed to show
again last night. Just as well, as we have made more progress. I am
confident I can take this thing quite a ways down the road now regarding
the bodywork. There are gaps to correct on the doors, and I have a plan
to weld backing strips, then grind them to finished gaps. Nick may have
some other idea, which would be good. Otherwise, that’s next on the body
list. To repeat from a few days ago: I have to get the column and brake
pedal in. We’ll do that shortly, maybe even tomorrow.
The hood lift system
works fine, and puts the fenders RIGHT back in place. There will be only
a slight amount of fabbing to do on the lower edges to get them to mate
exactly, and some centering devices to drop them into place every time.
9/25/11
Nick showed up
Thursday, and was highly complimentary, He repeatedly said “GREAT”
regarding what has been accomplished.
This is good.
I pressed him for
some additional hints as to how to proceed. He again suggested cutting
out the wheel wells, fabbing rod, and bringing the metal back to the
revised opening. I now recall I did this exact thing on the Funnycar
about 15 years ago, and of course had never done any such work prior.
This was in fiberglass. Now we’ll do metal. Nick offered to lend me a
hammer and dolly and shrinking hammer. I need him to show me how to use
them.
JJ and I did not get
to the steering column or brake pedal assembly. As I am now just about
broke, as in owing thousands more than I have, I may have to stop JJ’s
involvement, unless he wants to work on a credit for when some lump sum
of money lands.
Nick may go with me
and Bill Marigold to Winfield’s show in Mojave in 2 weeks.
9/26/11
JJ has consented to
work “on credit” until I get some cash again.
We 3 jumped on the
door gapping today, and essentially got it all done in metal. There will
be, of course, some minor bondo work to perfect the edges and levels.
But in our case, VERY little.
We cut the drip
rails off, then started adding 18-gauge shim strips. It turned out not
to require as many as I first measured, given the heat, welding, etc.
But we ended up with 2 layers in many places, and a few areas took 3
shims.
JJ cut these from
our sheet of 18-gauge, I easily bent them to fit, and started
tack-welding. We then came back and started grinding as needed.
The final gapping
looks like this:
So I COULD do some
bondo work now just to make it look better, but I think I’ll wait until
Nick has seen this stage and approves
We got both sides
done.
I noticed the front
clip sheet metal flexing over the subframe surrounding the grille area
slightly when I tipped it forward and rested the nose on a milk crate. I
had beefed this area up previously with some results, but I saw that
even more tying together was needed. This is mostly due to the fact that
the welded seams connecting the front metal to the hood/fenders/subframe
are incomplete. I will start on completing that tomorrow, but will add
some metal from the existing onto the subframe, after I do a little more
welding on those earlier seams.
I also added some
beefing to the front hood support in the middle, and this first picture
shows before the addition of the center “beef” plate:
Here it is after the
center plate install.
I will tie the front
sheet metal more securely to that subframe tomorrow.
I spoke with Preston
at Tammy Allen’s Museum, and brought him up to date on my project and
the Joe thing. He said they appeared to be going the same road, not
going after him for their money, just looking to get their cars back. I
offered to help that happen, and also suggested I could manage the
completion of those projects here using expert people. Allen has a
museum and presumably a serious shop attached to it, so may not need my
help there.
9/27/11
JJ and Kelly and I
continued today, addressing brake pedal mounting and steering column. We
were all ready to weld in supports for the brake pedal assembly when I
realized the steering column will need several u-joints, and the column
path may interfere with the brake location. So we switched, did some
mock-up of the column (just a short little 16” head unit), and kept it
bundled up in its foam wrap and foam box cover. We cut open the floor
for a 4 x 5 opening, and determined 3 more u-joints and two support
bearings are needed.
I will go to Hawaii
Racing tomorrow for those. Given that we can get these mounted, I’ll
need to come up with a column drop of some sort and front support for
the head to mount it all.
The doors look good
gapped, Nick did not show, so we continue on.
I finished the day
spending about a half hour solid welding under the front clip. Got REAL
hot there! I’ve closed most of the gaps in the front sheet metal
attachment to the “core support”. I may divert to other aspects of the
front end strengthening as needed tomorrow if things get slow.
9/29/11
oving the mondo plate I welded into the body. So
some panel replacement is in order there, about 4 x 6, no biggie. I will
buy another column drop per PBB’s thought, and build another stop up
there.
The steering wheel
runs through from side to side smoothly now, with no weight on the
tires.
I called JJ, and we
worked out his three issues. We have concocted some code names for each
of the three offensive actions, and he will clue me in when I do them.
It’s all about
communication.
Per Kelly’s
insistence, I added two flat bar bracing pieces at the front upper
corner of the brake pedal mounting area. This added a very small amount
of stiffness. The major wobble in the column is near the bottom between
#3 and #4 (from the top) joints. I am adding another Heim joint there.
10/6/11
I added the fourth
Heim, tightened up the column drop, and it is quite good now. I cut the
old lower left mounting plate right out of the body and relocated it. I
will now take the brake pedal assembly and remount it 1.5” higher,
rotate the upper Heim joint, and relocate the #2 Heim joint up to an
upward mount, cutting out the rather nice three-legged affair I just
welded in.
So goes the process.
10/7/11
I cleaned all the
column stuff out save one Heim mounting. I ordered a 7” drop from
Summit, so I will have to wait until mid-week to continue. It looks like
I can eliminate two Heims, perhaps three, and at least a couple of
u-joints.
The brake pedal is
back in, higher.
I moved onto the
hood area and am filling in the welds at all the seams, grinding as I
can, “healing” the stitches if you will. I have difficulty getting the
MIG to weld below about 15 amps, which of course burns holes in the
sheet metal. I tried 12-14, and it just doesn’t do it. This is where TIG
would be better. Perhaps I’ll try the torch next week.
Power Brake Bob has
some interesting (and good) ideas on the exhaust. He suggests using 6
boat mufflers, each about 5 x 12. I think I might be able to squeeze
them under the motors, with at least one each in the front cavity of
each pan.
10/9/11
PBB called today and
said he had pitched a sponsorship exhaust system to Gibson, who appeared
warm to it. So we’ll get the steering back in, and if Gibson says yes,
we’ll get it on a trailer to Corona later in the week.
Nice going PBB!!
Also saw Gene
yesterday and Bob today from BE Customs, and we chatted about the
progress on the KK. Bob said give a shout when I needed help. I
IMMEDIATELY said “help.” I have NO funds for their expertise, so other
than a mercy visit I see no work being done by them in the near future.
10/10/11
I talked with Joe
Ziola who asked that I check with him on Wednesday, pick him up, and
bring him over. He is no longer allowed to drive because of his seizures
emanating from a lifelong brain tumor. He appears to be recovering
nicely from really trick brain surgery, and looks forward to coming over
and being involved. He has a small 100-volt TIG machine, which I might
be able to use in his absence.
I’m at a standstill
right now waiting on the column drop. PBB is returning tomorrow night,
and might get going on the plumbing for the air brakes on Wednesday or
so.
It appears the
column drop is coming from New Jersey, so I don’t expect it before
Friday.
3:44PM
Got the Borgeson 7”
column drop in the mail on Friday, and upon opening it today realized it
was a 2” diameter, not 2.25” as I need. So I reordered the correct one,
and sent the first back to Summit. This puts the column on hold until
the new one arrives. Summit said they might 2-day air ship it. Whatever,
PBB can start in the brake lines, mounting the master, the tank, etc.
starting tomorrow.
I did some judging
with Randy and others at the Fire Dept Car Show yesterday, and the Best
in Show truck happened to be parked next to me, and had a trick
double-action hood slider and tilt. The owner, Phil, is supposed to be
coming over to look at the KK. I’m anxious for someone else’s eyes to
look at the mechanical challenges and see different solutions.
11/2/11
Spent two days at
SEMA and Apex, and I am EXHAUSTED. I have not done that much walking in
the last TEN years!!
The explanation of
the KK (no pix were handy) had a LOT of people interested I handed out
perhaps 25 cards, got a lot more than that, tons of literature (well
many pounds of it), and spoke with many people who had some interest and
good products for the project.
But this just KILLED
my back. Wow.
I also found the
Miller booth at the end of the second day (a WAAAAAYYY long story), and
they did not have a good enough deal on their new Diversion TIG machine,
so I passed. I’ll pick up my old EconoTig tomorrow, and start trying to
weld as possible with it. Sadly both my welders are not suited for
low-heat applications, such as EXACTLY what it is I’m doing with
18-gauge metal on the KK.
PBB is working the
show using the truck as a hook, and claims some interested parties there
as well. He will stay through Friday (I’d be dead by then).
11/6/11
I was wrecked from
two days of non-stop walking through Apex and SEMA. I came back to tune
up the welders. The TIG does not seem to weld at all, just spark like a
spark plug, then explode the metal in about 5 seconds.
The MIG is going a
better job, as I replaced some parts on it.
I have been unable
to get Joe Ziola over here yet to try the revised and repaired TIG.
Hopefully his chemo and radiation are not knocking him down.
I ran some welds on
the hood yesterday with the MIG, and will go out in a moment and do
grinding to see how they did.
PBB claims that
Gibson has agreed to do the exhaust, and had some potentially fruitful
conversations with a couple of other suppliers, both from an idea and
product standpoint.
I was driving
yesterday next to a late model VW and noticing how the headlights sit.
They are indeed horizontal and parallel to the road with the grooves
inside the housing. So I need to create some arrangement to adjust the
headlight body and get some metal work going for the “dormers” behind
them. I have no idea why in the hell Joe wasted time pounding and
stretching the fender around the left headlight, it just is nowhere
close to doing what is needed. More jerkness discoveries await, no
doubt.
The steering is in,
so PBB can commence his brake work this week. He is scheduled to return
some time this afternoon.
OK, off to the
garage.
11/9/11
So Kelly and JJ and
I have spent the last three days working the front sheet metal, as in
polishing it, welding, grinding, adding, cutting, etc.
We have narrowed the
gap from the hood to the cowl to 1/8” or less using metal only. We have
a little more tuneup to do there, but it is quite nice in pure metal at
this point.
The plan is still to
take the KK to Bob’s Big Boy on Friday, IF NO RAIN. That would be
disastrous to the fresh metal. We will likely put a couple of cans of
clear lacquer on the metal Friday to be safe.
Kelly and JJ are
both amazed at what we’ve done, and both are bullish on just trying
anything that needs doing.
The headlights are a
disaster. The right unit is broken in several places, has no good bulbs,
and is scratched up.
The left needs a
Xenon bulb.
I am checking with
PBB as he gets Bosh and wholesale, for a price on two new lights. We
MIGHT just use the lens, and substitute some other, simpler setup
behind.
The bodywork is
coming along as noted above, so we are going to press on come Friday.
PBB and I will
prepare some solicitations/proposals for four
sponsors this coming week.
11/10/11
Randy looked in on
the KK this afternoon after the NHRA drags, and said he was shocked and
amazed at what we had accomplished. He added, what we have done is very
good.
So, on we go.
11/17/11
Kelly and JJ and I
have put in some serious time this last week. I have spent MANY hours
ferrying my TIG welder back and forth to DeltaTech getting it FINALLY
fixed. First it was the board, then it was the pedal wiring, then
something else, and finally the high frequency polarity was incorrect.
Anyway, I am now learning to TIG weld.
During this, we
finalized the side panels, building ¼” square frames and sheeting them
with 18-gauge metal.
We then had to make
a step out (about ¼”) panel using some 1/8” flat stock on top of the
front portion of the panel, and again covered with some more 18-gauge.
This mated up the
faces of the two filler panels between the bed and the cab. Much on and
off the truck, grinding, back on, etc.
The steering needs
to come out about 3”, as I test fit the old dash back in, cut out for
the column, and the head needs to come back. So I need to remake the two
column drop mounts, and put a longer piece of “D” rod in to allow this.
PBB and I have not
yet done the sponsor letter. He has planned for his kid, Matt the
videographer, to come and film an install here, and do some KK filmage.
I have 7 hours of video, and untold hundreds of pictures along the way.
I will now need to
organize those to allow Matt to do some compiling of the data.
The right running
board needs a new top, so we will likely cut the old one off and fab a
new one. I WAS going to go over the old one, but I think not now.
We have to add
support along the back half of both running boards to prevent sagging,
etc.
PBB had some
thoughts today about two areas of the KK. Firstly, as he noticed us
beginning the construction of a tow bar system, he said I should
incorporate the battery box into that.
Secondly, he said I
need torque resistors of some configuration to prevent the crossmembers
and frame welds from suffering under a half ton of torque. He is right
about that, and I HAD bought and designed such a system. But then I
realized I had to allow for exhaust, and came up with a narrower
mounting system. But PBB is correct, so once the exhaust is finalized
(by Gibson we hope, and soon), then I can get on with the final
stren gthening, X-members on the frame, etc.
I am going to pass
on Bob’s tomorrow, as I have a family dinner at 5 PM ion Brentwood. But
we should have the tow bar done shortly, and I’ll need to go to
Eckhart’s to get a dropped hitch for the dually.
The tow bar at this
point will be bolted in with (4) grade 8 bolts, 5/8” x 5”. I MIGHT be
able to alter the design and do what PBB suggests, either tomorrow or
later. This would require making a separate bolt-on tow-bar receiver
piece with tabs to bolt onto the bottom of this crossmember arrangement.
11/18/11
JJ got the Grade 8
bolts, and Kelly and I finished up the tow bar. Once ready to final
weld, I realized it was about 3” too close to the ground. So we
shortened the legs, and welded in the center section, with tabs done and
complete.
Looks good.
It is now close to
being able to do the PBB-recommended battery tray/crossmember thing.
I’ll show PBB tomorrow and see what he thinks.
I got some practice
in last night on the TIG. I need MORE practice. LOTS more. Welding the
heavy tow bar stuff today was a joy. Just pour the current (set to 24
volts) to the beautiful open V-grooved weld pockets, lay the wire down
at the 40-speed setting, and rock. NICE. This is what I would like to do
with the TIG on the sheet metal patching. I need to call AirGas tomorrow
to see if my .023” rollers came in.
I went to Eckhart’s
and got a 10” dropped hitch arm and 2” ball, good for4 5000#, as the
actually-needed 12” was just too low. I need to put the license plates
on to tow it on the roads. Good thing the registration is current.
I MIGHT consider
taking this to the John Force Show. I’ll do some calling to them, and
check with Randy and a few others for opinions.
PBB has not yet
started on my brakes.
I will probably now
move to mocking up some seat, order the Old Air AC unit (unless I can
get them to sponsor it), and extend the column backwards about 3” or so.
11/19/11
PBB was busy doing a
brake job today. We will discuss the battery box and some other aspects
tomorrow. Nick dropped by and again expressed high praise for what we’ve
done. He again suggested doing a cage around the fender to finalize
that. I will get on that shortly. He thought bringing in a welder by the
hour might be a smart thing.
The TIG is operating
better, and Ziola will be coming tomorrow to view it, and my virginal
attempts with it. I do much better with a MIG right now.
Matt Sweeting was
here to film Bob and me. Bob ran late on the job, so Matt will return
probably Monday. Matt suggested several web-based things to promote the
KK.
11/20/11
Got Joe Ziola over
today to look at the TIG welder, watch me weld, and show me some tips.
All of the above were accomplished. He thinks the MIG is faster and
easier for most of what I want to do. The TIG will allow me to do some
small, sensitive stuff, once I get the hang of it.
11/21/11
I ran a few minutes
of TIG this afternoon, getting a little better. I’m not quite ready to
use it on the KK as yet. I will get the .023 wire rollers tomorrow, and
see how the MIG does with the smaller wire.
PBB is booked until
Wednesday, AND we cannot find the air/hydraulic power booster. So he
will have to procure another.
The weather for the
end of the week is predicted to be rainy, so Bob’s using the tow bar is
unlikely.
I will call Craig at
the John Force Car Show and ask if the KK would be appropriate.
I will get into the
fender “cages” soon.
11/23/11
I have attempted to
get the TIG and MIG welders to work on sheet metal, so as to nicely
complete panel changes, etc. I have small Tungsten in the TIG, smaller
rod, and .023” wire in the MIG. I went to change the rollers, and the
retaining device broke off. I installed it anyway, and I’m hoping this
will work well enough to get me through until next Wednesday, at which
time a replacement mechanism should arrive. Yuk!
Matt Sweeting filmed
me and the truck last night. I have yet to see any of the footage.
11/29/11
I FINALLY attacked
the front fender conundrum. I cut the bottom approximately 1” off them
to match the underside of the body and the lower edge of the running
board.
I remade the ½” solid
round bar Joe had put in there, changing the shape a bit. I then welded
(per Nick’s recommendation) the sheet metal to the upper back edge of
the round bar. It looks
quite nice now. It is a solid-welded front seam, som back welding, and
pretty smooth now.
The “landing pad”
for the lower edge of the fenders will be 3/8” plate, welded to the
underside of the front edge of the running board. I have fabbed a new
front edge and under-support, gapped the distance to the fender at about
1/8”, and we’ll pull the whole thing off tomorrow to add three rear
braces, another front support, and weld it all up nicely.
SO in six months, we
have made some SERIOUS progress, tightening up a lot of stuff. This is
the surprising part to me, as I had NO idea I could do any of this.
Not that I would,
but if the thing were to go to bondo right now, all gaps would look damn
good.
I SO want to smooth
some areas with plastic, but this is WAY premature. So I keep attacking
the stuff I feared the most, and knocking it out.
PBB cannot find the
air master and booster.
12/1/11
Man, we are on fire
today. I mean LITERALLY. I lit my sweatshirt on fire from grinding
sparks,
ried to put it out
with my left hand, at which point the shirt MELTED onto my 4th and 5th
fingers,
and continued the
destruction. This went through my sweatshirt, inner shirt, and just
touched my stomach. My fingers did not fare as well.
We then continued
(after holding ice on my fingers for over a half hour) with tuning up
the left running board. We got the pilaster finally SOLID and straight,
and added a shim piece to the forward side. We also added the under
braces to the rear half, put in three ¼” x 1” kerfed curved steel braces
for the front, middle (around the curve of the cab), and rear edges, and
ground off a lot of rough welds, etc.
The left running
board is back in now, and once we put braces in the LF fender, we’ll
finalize the gap at the front of the
running
board. Right now it is about 1/8”, but we have to stabilize the fender
before we sheet the top of the front of that running board. JJ is
kerfing those braces right now.
20-installed
stiffeners under the cowl and on the firewall
21-set the motors
back in (not final alignment)
22-arduously cleaned
the wheels of 5 years of exposure to the chromed and polished surfaces.
The tires are now junk from weathering, although they were brand new.
23-welded the rack
mounting back secure
24-cut/caged the
front fender bottoms to align with the bottom of the running boards and
body
12/16/11
The KK is sitting at
Bob’s. We will be going back in a few hours to sit with it for the
evening. All went well getting it there.
Things went well at
Bob’s including one fellow who wanted to contribute money to the
project, in the hundreds of dollars, for a spot on the contributor
placard. That’s a wonderful response to the car! It got LOTS of
interest.
12/19/11
Another breakthrough
day on the bodywork. I cut the wheel well out of the right fender, and
created a new opening. We will weld in the new rim tomorrow, and add
some metal to cover some gaps. This has freed up the front end design,
and eliminates a sticking point for me on the way the wells looked.
12/20/11
Today we attacked
the LF wheel well opening:
The opening, made
from solid 3/8” rod, is welded in on the inside. We’ll fab up the front
filler and beat the rear quarter piece into the revised shape and weld
them back in.
I’ll need to
reinstall the two removed flat braces from both fenders.
Next we’ll attack
the lower portion of the cowl where the fender comes down. I cut those
shoulders loose and pushed them in for clearance.
12/22/11
The second time
around on the left front fender looks good. I did some additional
welding of cuts, etc., and JJ ground those down. We also final-gapped
the right side of the hood at the cowl, all the way down to the fender.
This requires a LOT of small welds, cutting, and grinding. That gap now
looks great.
PBB did a little bit
of brake work tonight. I welded in three tabs for him, ground the welds,
and did all I could on those tabs. He needs different fittings to route
the lines in the most attractive way, per my suggestions. So no more
will be done on the brakes until mid-week next week, once fittings are
sent.
We are going to use
a through-the-frame bulkhead fitting to allow us NOT to go under the
frame rail. Safer, and much more attractive.
I am going to Bob’s
Toluca Lake again tomorrow, for our second time there. The manager,
Mark, is departing his career there as of tomorrow, so henceforth it
will be Leo who will be the go-to guy. Leo likes the truck and me, and
wants me to consider bringing it to their new once-a-month Saturday
night thing.
12/24/11
Met with Mark. NICE,
NICE GUY. We’ll be in touch regarding him selling solar for me.
The install went
well, as did the leaving later on. LOTS of questions, lots of interest.
This inspires me to get moving on getting it running. PBB has to get
more fittings to continue on the brakes. I can move on the steering
column. We adjusted the front end today and got it nearly dead tight on
both sides. As soon as we install the alignment pin system, that all
will be handled. The more user-friendly lift system switches worked out
great mounted to the radio portion of the dash panel. The air board has
one leaking fitting. I’ll address that tomorrow.
I think I dropped
the trailer hitch receiver pin lock keys on the bumper and drove away
after dropping the KK back at the house tonight. Against my wishes,
Kelly had me keep the three keys together. Now, not so good an idea.
JJ and Kelly and I
are all stoked on the art deco approach, and the three blue glass fins
in particular. This is fun.
12/25/11
I drove the route to
ColdStone and back looking for the keys. No good.
So I’ll cut the
hitch off and get or use a simple pin and clip.
We are sending off
some info to Stacey David for possible mention on his show.
Bob is making a list
of SEMA vendors appropriate to sponsorship on the KK. This week will see
us actually doing construction work, so this will dent our time on the
KK. I was getting used to this being my everyday job.
I don’t foresee Crow
actually doing much on the project, notwithstanding his interest,
capabilities, and talk. He has his own shop to maintain.
We carved the rear
fenders’ trialing edges to allow for removal of the rear tires when the
bed is raised. They look GOOD. More and more little refinements are
adding up to some noticeable improvements.
12/27/11
I nipped off the
hitch pin, so that’s done. JJ and I looked at the right running board,
and I started in on bending the kerfed ¼” x 1” bars for the front and
rear ends of the board. I got the rear done, and then noticed the fender
does not stay level near the outer edge of the running board. I have a
½” wood shim under the fender where it goes under the bed, and this is
partly kicking up that front corner of the fender lip. I did it to gain
clearance for the tire. I now find the tire/wheel has been spaced out
about a half inch by spacers and nuts to achieve this clearance. I’ll
try removing the spacers behind the wheels FIRST before carving up the
fender. I may still need some fender adjustment, but the wheel offset is
an issue unto itself. I have some spacer plates which I may employ here.
I prefer to just eliminate the spacers and gain a little breathing room
on the fender clearance. This is particularly important as the front
wheels have a much deeper recess from the fenders, and this extra space
does not look good to me. I am unafraid to modify the fender given what
we’ve accomplished in the last week. But why do it if it’s not
necessary?
PBB has asserted his
belief that the front A-arms can be adjusted OUTWARD to tighten up the
front wheel and fender clearances.
JJ and I noticed
that the fender modifications we did made a substantial difference. The
front wheel wells look much more balanced, and took away some of the
hooding of the front tires. I makes the truck to a[[ear two inches
higher, which it is not.
This is good.
I MIGHT jack the
front up an inch or so at some point. For now,k it fits nicely.
The hood also fits
well. However, the bed has started shifting about an 1/8” to the right
on closing. We do not yet have alignment pins in place, which would cure
this. But perhaps some massaging of the pivot holes (AGAIN) might be
needed. I really don’t want to mess with the pivots at this point, as
the front gaps are at super-tight 1/8” reveals. There is NO room to mess
around.
All part of
tightening up the gaps and fitments.
The right door began
NOT latching a week ago . The latch is buried in the door, and is
difficult to see, even with a light. Apparently a wire strung through a
piece of metal was hooking itself on a lip of sheet metal inside,
causing the locking latch not to drop. I also needed to move the strike
pin on the jamb to the outside about 3/8” (grinding it out) to get the
door the close flush.
All good again.
12/29/11
The right rear
fender has received some attention: with removing shims, setting the
rear wheel in about ½” and preparing the running board for remaking, we
found the fender was off too far for good taste. So I cut out the
leading corner, put in a new lower rod (WAY too much work, and didn’t
end up being where it was needed), and POUNDED the new piece into shape.
I mean really pounded on it. It took most of the morning, and it is
welded in. I further hammered and dollied on it to get it more
appropriate. It looks good, and I now have made a new rear ledger, if
you will, to carry the trailing edge of the running board at the fender.
I’ve got the gap just about 1/8 for most of the fender. The fender
itself has a dip in the middle, which will get filled eventually. I’m
debating about putting more metal along that edge.
For now: NO.
Kelly and I pulled
the running board off, and put it back on, 3 round trips. I got the new
ledger around the back of the cab PERFECT, after two tries. I added to
the vertical and horizontal portions of the 1.4” x 3” angle iron
structure, and that has tied it all together there. We also got the 6
stiffeners under the rear portion of the running board, and that has
straightened that right up. I still think I’ll resheet it. Nick
suggested going to heavier sheeting, like 1/8”, and again reiterated his
opinion that we are doing great on this. I know nothing about shrinking
metal with heat and quenching (have not tried it), and asked him for
some pointers.
Nick also commented
how nice lead would look on a lot of the metal. So I am going over right
now to get some from him.
I am
building a new shoulder area to receive the fender, and it looks good so
far.
Randy came by Friday
and just dubbed us the Metal Maniacs. He remains impressed, and
reiterated we are doing good work, way beyond his comfort level.
The bed closes the
same each time now, and I need to trim the right front panel to regain
the 1/8” gap I had before the bed relocation., The corbels line up
nicely, and I’m tempted to bondo the lower portions to see how they
really match. I need some alignment pins first, of course, the mate the
bed reliably to those corbels. I’ve tuned up the running board on the
right, as in rebuilding it, and the lower panel fits pretty well between
the running board and bed, but needed to move back about an 1/8”. The
trailing edge of that panel needs a little build-up to match the revised
curve of the rear fender.
JJ and I picked up a
sheet of 1/8, some flat, that fence 2x2, and more round stock.
Randy noted concern
for the overlapping ramps I have on the lift, feeling the edges were not
rated for such loads. So I beefed up the ends of them with lots of steel
and feet of welds, and used up the remaining gas in the MIG tank. I just
filled that a couple of weeks ago! Perhaps leaving the valve on
overnight from time to time was costly. Lesson learned.
I’ve left several
messages for Rob Moore about completing the transfer case. I will hound
him this week to get the finished case done, and then send him a CV
joint for final quote, and hopefully the making of the two short shafts.
Salim dropped by,
was amazed at what we had done, and provided P{BB another forum for how
we need to augment the mounting of the engines. Yeah, yeah, but after
the exhaust gets done.
PBB has received the
bulkhead fittings, and we’ll drill the frame tomorrow (9/16” diameter)
tomorrow for those two fittings.
1/10/12
Got the two bulkhead
fittings, in, and ran some brake lines to the rear. Bob temped up a
piece for the front run, involving some curves, and will attend to
making the real line tonight. He needs a little more line for the
crossover runs.
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